Posted on 02/04/2003 1:34:19 AM PST by bonesmccoy
In recent days the popular media has been focusing their attention on an impact event during the launch of STS-107. The impact of External Tank insulation and/or ice with the Orbiter during ascent was initially judged by NASA to be unlikely to cause loss of the vehicle. Obviously, loss of the integrity of the orbiter Thermal Protection System occured in some manner. When Freepers posted the reports of these impacts on the site, I initially discounted the hypothesis. Orbiters had sustained multiple impacts in the past. However, the size of the plume in the last photo gives me pause.
I'd like to offer to FR a few observations on the photos.
1. In this image an object approximately 2-3 feet appears to be between the orbiter and the ET.
2. In this image the object appears to have rotated relative to both the camera and the orbiter. The change in image luminosity could also be due to a change in reflected light from the object. Nevertheless, it suggests that the object is tumbling and nearing the orbiter's leading edge.
It occurs to me that one may be able to estimate the size of the object and make an educated guess regarding the possible mass of the object. Using the data in the video, one can calculate the relative velocity of the object to the orbiter wing. Creating a test scenario is then possible. One can manufacture a test article and fire ET insulation at the right velocity to evaluate impact damage on the test article.
OV-101's port wing could be used as a test stand with RCC and tile attached to mimic the OV-102 design.
The color of the object seems inconsistent with ET insulation. One can judge the ET color by looking at the ET in the still frame. The color of the object seems more consistent with ice or ice covered ET insulation. Even when accounting for variant color hue/saturation in the video, the object clearly has a different color characteristic from ET insulation. If it is ice laden insulation, the mass of the object would be significantly different from ET insulation alone. Since the velocity of the object is constant in a comparison equation, estimating the mass of the object becomes paramount to understanding the kinetic energy involved in the impact with the TPS.
3. In this image the debris impact creates a plume. My observation is that if the plume was composed primarily of ET insulation, the plume should have the color characteristics of ET insulation. This plume has a white color.
Unfortunately, ET insulation is orange/brown in color.
In addition, if the relative density of the ET insulation is known, one can quantify the colorimetric properties of the plume to disintegrating ET insulation upon impact.
Using the test article experiment model, engineers should fire at the same velocity an estimated mass of ET insulation (similar to the object seen in the still frame) at the test article. The plume should be measured colorimetrically. By comparing this experimental plume to the photographic evidence from the launch, one may be able to quantify the amount of ET insulation in the photograph above.
4. In this photo, the plume spreads from the aft of the orbiter's port wing. This plume does not appear to be the color of ET insulation. It appears to be white.
This white color could be the color of ice particles at high altitude.
On the other hand, the composition of TPS tiles under the orbiter wings is primarily a low-density silica.
In the photo above, you can see a cross section of orbiter TPS tile. The black color of the tile is merely a coating. The interior of the tile is a white, low-density, silica ceramic.
2. I.e., is fatal elvon burn-through a more frequent potential occurance than discussed so far?"that is the only case I saw, however, it was so serious they changed the tile layout and types of tile in that position. and now ..... dah dah dah - I heard, they hadn't done it on the colombia, yet.
That would really be interesting, but I'll wager it will never happen.
That and nothing really out of the ordinary until the breakup.
Was it XBob that posted about the near burn-through on a super steel rod in this thread?
This reminds me of that, in a way. Very sudden.
That and nothing really out of the ordinary until the breakup.
Was it XBob that posted about the near burn-through on a super steel rod in this thread?
This reminds me of that, in a way. Very sudden.
Yes, that's because these "prints" are terrible. It's held in place by tight tolerance and pressure from bolts and it looks like some heavy springs, but it's not at all clear. If it's to be believed they have a CarpA bolt going though the SiC layer of the RCC section. ?
I'm just working on the assumption that perhaps a piece of the RCC came off early. I'm probably way off base.
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