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Boeing should have spent more time on the plane the altogether-new competitor plane they were intent on building rather than rushing along with 'upgrades' to the 737 which mess with its aerodynamics and software supposedly meant to offset it.
1 posted on 04/09/2019 12:49:46 PM PDT by CondoleezzaProtege
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To: CondoleezzaProtege

Rush should stay away from the technical stuff.


2 posted on 04/09/2019 12:55:23 PM PDT by TexasGator (Z1z)
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To: CondoleezzaProtege

The latest version of the 737 is probably the ultimate limit stretch of the 737, but it is an outstanding aircraft .

The only real problem with the upgraded 737 is the augmented stability system used to allow the upgraded 737 to mimic the same flight characteristics as the older models to the 737 to allow pilot trained on older models to fly the newer version with minimal retraining


3 posted on 04/09/2019 12:59:44 PM PDT by rdcbn
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To: CondoleezzaProtege

This explanation says to me stick with politics Rush.


4 posted on 04/09/2019 1:01:11 PM PDT by rockinqsranch (Dems, Libs, Socialists call 'em what you will they all have fairies livin' in their trees.)
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To: CondoleezzaProtege
As smart as Rush is, he doesn't know much about what Boeing actually did. Even though he's an aviation enthusiast, this is just laughable...
"The nose gear was actually eight inches longer to accommodate the bigger engines. So it changes the elevation of the nose of the airplane as it’s flying through the air..."
Boeing DID lengthen the landing gear, but obviously the gear are retracted in flight and do not affect the flight dynamics.

When Boeing adopted the higher-bypass LEAP engines to get improved fuel economy, they now had a ground clearance problem -- the engines were simply too big to fit under the wing. So they did two things: lengthened the landing gear AND moved the larger diameter engines forward to get the nacelles in front of the wing. In normal attitude flight, the nacelles do not generate lift, but at high angle of attack flight, they DO generate lift. Because they are further forward, this lift generates an upward pitch moment. The problem is that the upward pitch in high angle of attack flight is not what you want because it exacerbates the situation. Higher angle of attack attitude --> more upward pitch moment --> higher angle of attack --> more upward pitch, etc. (think of this as a positive feedback loop). This can happen very quickly, too, and is NOT the handling characteristic of the more neutral prior 373 types.

MCAS was added to arrest this upward pitch tendency in high AoA attitude flight. If they hadn't done this, the 737 MAX would probably have required complete re-certification as a new airframe (no longer the 737 type) at untold millions and years of delay. It was a bad FINANCIAL decision at the expense of safety.

5 posted on 04/09/2019 1:01:25 PM PDT by ProtectOurFreedom
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To: CondoleezzaProtege

I’m sorry, but Boeing used software as a cheap way to try to compensate for an inherent design flaw.

The aircraft is simply not airworthy. It’s natively tail heavy and the aircraft is in many ways significantly different from the preceding versions of the 737 that it should not be called a 737. I say that because a pilot who is used to a 737 is not going to be able to just sit down and drive a 737 Max without a lot of required training and without a lot of training on how to drive the thing without the MCAS.

What makes these aircraft so dangerous is that if they lose power the aircraft can’t be controlled by the crew in the same manner that a normal 737 can be controlled by a crew in a similar situation.

It’s not a safe aircraft and I will not get on one nor will anyone in my family ever set foot on one.


6 posted on 04/09/2019 1:02:30 PM PDT by MeganC (There is nothing feminine about feminism.)
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To: CondoleezzaProtege

Boeing effed up hard and 500+ people are dead.

https://www.youtube.com/watch?v=dBWGjT-XV6g


8 posted on 04/09/2019 1:03:07 PM PDT by mylife (The Roar Of The Masses Could Be Farts)
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To: CondoleezzaProtege
Boeing should have designed an all-new wing for the 737 MAX instead of adapting the 737 Next Generation wing design.

The A320 Family design had its share of problems: the freezing pitot tubes caused a couple of crashes due to interfering with the fly-by-wire control system. That's why Airbus had to redesign the pitot tube heaters. And it's only now that Airbus finally got reasonably reliable Pratt & Whitney PW1100G engines.

9 posted on 04/09/2019 1:07:13 PM PDT by RayChuang88 (FairTax: America's Economic Cure)
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To: rockinqsranch; ProtectOurFreedom; T-Bird45

Here is one take I’ve read:

“It has already been well established that the new Max version of the 737 has greater tendencies for the nose to climb higher under heavy thrust conditions than previous models. There appear to be several factors that may contribute to this. When this plane first came out back in ‘69 or so, the point where the thrust from the engine met the surrounding environment (push point as I call it) was well behind the wing, and vertically very close to the wing’s rotation axis with the long skinny JT-8 engine. When the larger diameter CFM 56 engines were later installed with 61” diameter fans, this “push point” was moved near the front of the wing, but it appears this was not enough to cause serious handling problems.

Because the engines of the new Max version now have a fan diameter of 69 1/2”, and are 21” longer, (124” vs 103”) the engine and push points have been moved forward yet again. I recently overlaid 2D CAD drawings for both planes, and discovered that the exit point for the thrust from the bypass shroud has been moved forward by 22”, and the exit point for thrust generated by the LP turbine has been moved a whopping 29” ahead of the old locations. The leading edge of the nacelle is now 13 1/2” inches ahead of the old location. The axial center line of both engines is roughly the same, with the additional diameter being divided equally above and below the old location.

So from a purely mathematical perspective, as long as the plane is flying relatively flat at high speed, this horizontal shift shouldn’t have much effect, but now that both the LP and bypass thrust points are much further forward than before, and the LP/bypass ratio has changed, the effects of this could be fairly dramatic under certain conditions.An example would be if the plane is oriented at a pitch of say 45 degrees, but flying at a low enough speed that it’s trajectory is still roughly parallel to the ground plane, the downward projecting thrust from the engine would be would be at least somewhat deflected up and back and into the front of the wing as it traverses across the stationary air. This would in theory at least create additional lift at the front of the wing, inducing more pitch rotation forces.

Using the same two CAD models but this time oriented with a 45 degree pitch, some interesting things started to appear. The first is that the top edge of the bypass shroud outlet is now horizontally or slightly above the leading edge of the wing, (18” higher than the older model), and exits very close to the wing’s leading edge at this angle. How much effect this has on lift I’m not sure, but I was very intrigued by a photo of the A 320 NEO that showed where Airbus added long “ear” shaped extensions to the top (and bottom) of both the bypass shroud and LP exit point to deflect thrust away from the wing. (Boeing has a smaller one on the LP section only).

Another part of the equation that I noticed relates to the nacelles themselves in relationship to the axis of rotation. With the same models pitched at 45 degrees, the bottom of the nacelles are so much higher than the rotation axis of the wing root that they would act as lift devices for sure, and to some degree air brakes as well depending on severity of pitch. I measured the distance from the bottom front of the LEAP nacelle to the approximate centeroid of the wing root and found it to be 113” above, and 180” in front of the root center. The older version had measurements of 106” and 168” respectively, along with less surface area at the front of the nacelle where this potential leverage would be the greatest.

At first I didn’t think too much of it as the nacelles are rounded rather than flat planes, but the projected surface area of the nacelle is roughly 60% of the horizontal stabilizer, so there would be enough surface area to affect the dynamics of the plane. Regardless of whether my theories are correct or not, it is well known that this plane is not as aerodynamically stable as previous versions, as the implementation of MCAS was from what I’ve read, was apparently required for certification. Whether the plane is unstable enough that it truly requires MCAS to stay in the air, or whether it was only implemented to help the pilots deal with a few handling quirks under certain conditions, that I can’t say. If my theory on thrust deflection is correct, then a relatively easy fix for this plane’s stability issues may be to modify the bypass shroud for more lineal control of the thrust direction. If not correct, then there’s likely no fix to the stability issues other than re designing the entire wing root to accommodate longer landing gear, which is not likely to happen.” ~ Greg Miller


11 posted on 04/09/2019 1:09:25 PM PDT by CondoleezzaProtege
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To: CondoleezzaProtege
If they had just put new engines — larger but more efficient engines on those wings, because it’s so low to the ground,...and more forward.

Try some out of the box thinking:


12 posted on 04/09/2019 1:09:42 PM PDT by spokeshave (recovering Spokeshave from another computer.)
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To: CondoleezzaProtege

I.guess the average employed pilot know to keep his mouth shut on the 737MAX contraversy.


15 posted on 04/09/2019 1:47:27 PM PDT by cymbeline
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To: CondoleezzaProtege

All of this “Baseball, Hot Dogs, Apple Pie, and Boeing” rhetoric isn’t going to wash. Boeing is just as much of a quasi-governmental entity as Airbus, and its technology is falling behind.


28 posted on 04/09/2019 2:25:47 PM PDT by Mr. Jeeves ([CTRL]-[GALT]-[DELETE])
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To: CondoleezzaProtege
And if they were able to disengage the autopilot and disengage MCAS, then eventually it was gonna win and point the nose down, and that’s what happened.

What is this "it" he is referring too?

It seems to me if auto pilot, and MCAS are disabled a pilot would have to be concerned with the nose rising, and not be worried about the nose pointing down? - Tom

29 posted on 04/09/2019 2:38:28 PM PDT by Capt. Tom
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To: CondoleezzaProtege

This design was flawed from the beginning. It will become Boeing’s Edsel with a touch of Corvair.


46 posted on 04/09/2019 3:49:01 PM PDT by SERKIT ("Blazing Saddles" explains it all.......)
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To: CondoleezzaProtege

Payback for the sonic cruiser.

By the way - Rush is an idiot if he really thinks making the nose gear longer makes the plane fly in a nose up attitude.

“The nose gear was actually eight inches longer to accommodate the bigger engines. So it changes the elevation of the nose of the airplane as it’s flying through the air”


49 posted on 04/09/2019 3:56:59 PM PDT by PAR35
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