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To: SycoDon

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31 posted on 07/10/2006 12:59:49 PM PDT by kpp_kpp
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To: kpp_kpp; All
National Transportation Safety Board PRELIMINARY REPORT

On May 10, 2005, at 1930 central daylight time, a McDonnell Douglas DC-9-51, N763NC, collided with an Airbus A-319-114, N368NB, during taxi resulting in substantial damage to both airplanes near gate G10, at Minneapolis/St. Paul International Airport (MSP), Minneapolis, Minnesota. Both airplanes were operated by Northwest Airlines Inc. (NWA) under Title 14 Code of Federal Regulations (CFR) Part 121 as scheduled-domestic passenger flights 1495 (N763NC) and 1849 (N368NB). Visual meteorological conditions prevailed at the time the accident. Both airplanes were evacuated after the collision. N763NC's captain received serious injuries, the first officer received minor injuries, and a flight attendant received minor injuries. One flight attendant aboard N368NB received minor injuries. One ramp service agent received minor injuries.

N763NC departed Port Columbus International Airport (CMH), Columbus, Ohio, at 1826 eastern daylight time and with a scheduled destination to MSP. N763NC experienced a reported loss of right hydraulic system fluid quantity during a climb to cruise from CMH. The flight continued to MSP where a landing was made without incident. The flight then taxied under its own power to gate G10 where it stopped and awaited a tow into the gate while N368NB was being pushed back by a tug. N763NC then moved forward and impacted the right wing of N368NB. Both airplanes were evacuated using N763NC's rear airstair door and N368NB's front left slide.

Examination of N763NC's right hydraulic system revealed the right hydraulic reservoir fluid quantity was below "EMPTY," and the left hydraulic reservoir fluid quantity was above "FULL." The right side hydraulic system was pressurized with hydraulic fluid and a leak from the rudder shutoff valve housing was noted. The rudder shutoff valve, part number 3772374-5503 G, serial number RON 1185, had a recorded total time in service of 62,436 hours. The rudder shutoff valve was removed and sent to the National Transportation Safety Board's Materials Laboratory for further examination.

32 posted on 07/10/2006 1:12:19 PM PDT by oxcart (Journalism [Sic])
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